Saturday, June 10, 2017

180W Pallet Amplifier Using MRF9180


This is my first time to play with the 180W pallet amplifier kit from China. The kit comes with only a printed schematic but there was no details for the input transformer and the coaxial balun. The bias for the LDMOS is not also indicated so I have to download the datasheet of the MRF9180 from the internet.

The input transformer has a 9:1 impedance ratio so it has a 3 turns in the input while a single turn in the output. Connected to the drains are the 25 ohm teflon cables. This coaxial transformer is responsible for stepping up the low impedance drain to approximately 25 ohms. Next is a 50 ohm cable used to combine the 25 ohm balance signal into 50 ohm unbalance at the output. I choose to cut this cable to 15cm so that pallet operation would be optimal at the fm broadcast band.

The datasheet says that for MRF9180, gate voltage bias may be set anywhere between 2 to 4V but in my amplifier the VGS was set to 2.2V. At full output power, the pallet amplifier is consuming around 8 to 10 amps at 24V dc supply.


After the test, I was getting 150W at 144MHz (2W) drive and 200W at 100MHz (1.5W) drive and this pallet amplifier is remarkably broadband. The test was conducted without the LPF at the output.
--- 73 de du1vss.

Sunday, December 18, 2016

7MHz VFO using 3.58MHz Ceramic Resonator


This project is a 7MHz vfo that uses a 3.58MHz ceramic resonator. The oscillator output is fed to a frequency doubler but the output of the stage contains full of harmonics. To clean the output waveform, a double tuned band pass filter is added. Each filter resonates at 7MHz and the passband is quite sharp which effectively attenuate the unwanted harmonics.



The output level is at 3volts peak to peak and has a 60Hz per hour drift after some warm-up. Using 1N4007 as varactor, i was able to tune +/- 0.200MHz from the center frequency of the oscillator.   73 de du1vss

Tuesday, April 5, 2016

QRP RF Voltmeter from your Junk Box


A useful tool that can be easily crafted out from your junk box is this rf voltmeter. I discovered this circuit online and created a  prototype out of it. I found this project very useful in reading RMS voltage in my HF /VHF projects. I use it to determine the output power of my rf amplifier, set the null in my balanced modulator, determining the peak voltage output of my oscillator, peaking a band pass filter, etc... 

It takes only 3 components to start with. I use 1N60 germanium diode to rectify the high-frequency AC signal into a DC voltage compatible with any digital multimeter. My prototype rf voltmeter is mounted in a small PCB assembled in surface mount fashion. Two connectors soldered on the edge of the pc board to accommodate the positive and negative probe of my digital multimeter.


Connect the alligator clip to the common ground of the circuit you are measuring. Minimize the length of the alligator clip wire to avoid introduction of errors in your measurements, particularly on higher hf bands. In my prototype the lead wire for the alligator clip is just over 6 inches.


When reading the Vrms, take the measurement across the 50 ohm dummy load. For instance, if you measure 13V using your digital tester, the computed power is around 3.38watts, calculated using the formula P = (Vmeasured)² / 50.    ---73 de du1vss

Sunday, March 20, 2016

40M DSB Transceiver



The circuit described here is actually a variation of the  MDT40 project by VK2DOB,  A simple double side band suppressed carrier (DSBSC) transceiver which operates on 7MHz. I find this project simple and a good start if you are interested into home brewing your own rig so I decided to make one.

In the original circuit, it uses a ceramic resonator as a common oscillator for both receive and transmit stage but I have difficulty in finding the parts here in Manila so I decided to use a vfo whose circuit was copied from KD7REM, a rocksteady vfo. Stability is considerable during start up which usually takes less than 30minutes of wam-up and can be used with a couple of QSO without correcting the vfo for a drift. T50-6 toroid was chosen as a core of my inductor where 25 turns of enamel wire was wound. RF feedback was taken at 5 turns from the cold end. I found by experiment that by keeping the capacitance large in the L/C ratio, the oscillator is more stable than the other way around. MPF102 is also used since JFET is more stable than its BJT counterpart.

The balanced modulator and the receiver pre-amplifier stage are constructed together in one board. There are four 1N4148 used in the balance modulator and please note that these diodes are carefully matched by their forward bias voltage. A 500 ohm potentiometer is used to find the null in the balance modulator. Carrier suppression is easily done when you already have completed the transmitter stage since this can be just adjusted by the power output of the rf amplifier stage.


The rf transistors found  in the transmitter stage are uncommon so I decided to redesign completely the entire stage using common transistors that are locally available here. 2SC2078 was chosen as the final stage since it is cheap and offers a 4W to 5W ouput at the HF frequencies.




Above is the prototype of my DSBSC transceiver that I made. It is housed in a plastic casing (black) and on the top (grey plastic casing) is the additional 15watts linear amplifier constructed using a push-pull IRF510 mosfet transistor.  ---73 de du1vss

Tuesday, December 22, 2015

VHF RF Choke


Home made VHF rf choke. It has a typical value of 0.3uH made by winding 15 turns of 0.2mm enamel wire over a high value resistor (27K 1/2watt) as a former. Inductor leads are soldered across the resistor leads and the instant glue secure the winding on the former.



Most of my home made vhf rf amplifiers uses this rf choke in its bias and also in the DC supply section. Commercial vhf choke generally comes in a small package suitably for smd but since I have so many enamel wires in my junk box, home brew comes in handy.   ---73 de du1vss

Thursday, September 17, 2015

FM Broadcast 55W Push-Pull RF Amplifier


This prototype rf amplifier uses two 2SC2640 VHF power transistor wired in push-pull configuration. The 50 ohm impedance of the input is transformed to lower impedance by the 4:1 broadband coaxial cable transformer  providing a close match to the base of the two transistor.  To operate in class C, the base of the transistor must be at ground potential so the secondary winding of the 4:1 coaxial transformer is grounded at the center position( null).  The impedance of both collectors are transformed by the combination of  inductors L1 , L2 and the 120pF capacitor  and further transformed by the 1:1 coaxial balun.







Both the 4:1 coaxial transformer and the 1:1 balun are made from RG316 teflon coaxial cable and these are cut to a certain length in order to operate at the highest cut-off point which in this case at 110MHz. Actual test of the prototype amplifier, I was able to measure 55 watts output from a 1.5 watts input.   ---73 de du1vss

Friday, September 4, 2015

Quarter Wave Stub Demo

One of the trick that you can perform to your friend (not a Ham) is this quarter wave stub. Looking at the DC (direct current) point of view, the bulb should not light since there is a shorting wire (stub) that will ground any voltage present across the 12V bulb. But strange things happen when a strong rf source is brought near the dipole antenna. The bulb should light brightly! This phenomenon can be easily explained when we understand how the quarter wave stub behaves when excited at its resonant frequency.

In my prototype, I use a 435MHz  3w transceiver to excite the dipole antenna and the 12V pilot bulb was used as an indicator for rf current present across the feed point of the antenna. The antenna itself is approximately 13 inches in total length while the stub length is 6.5 inches. Spacing of the stub was merely approximated to around 1/16 of an inch. Part of the trick is that you can also cut open the far end of the stub and show to your friend how the bulb immediately off at this time.   ---73 de du1vss