Sunday, November 12, 2017
Home Brew Static Wick
By theory, this device bleeds excess voltage potential of your tower and thus minimize the risk of direct lightning strike. This device is totally different from the lightning arrester and though it does not guarantee 100% protection but there is no harm in trying.
I made my wick from fine stainless wire cut 12 inches long. I prepared 15 pieces of these wires then I folded it in half and crimped them together in a 3/8" stainless tubing. The more pointed tips, the better it perform so it is your option. The wick can be attached to the highest portion of your tower and must be provided with grounding below. 73 de du1vss
Monday, August 28, 2017
Diode Ring Mixer
40m band is poor today and I want to listen to the AM broadcast band. However, my IC-M700TY HF transceiver can only go down to 2MHz. Upon checking my junk box, I found the right components to assemble an up converter so that I can still hear AM broadcasts on my transceiver.
The illustration above depicts a diode ring mixer, In my prototype, I am utilizing four closely matched 1N4148 diodes based on their forward voltage and a pair of FT37-43 toroids as a core for my broadband transformer. The transformer is wound with four trifilar turns of #22 AWG insulated wire.
I've enclosed the finished prototype in a plastic container and I've installed a pair of connectors on the side for easy connection of the aerial antenna and the patch cable leading to the antenna connector of my IC-M700TY. The aerial antenna will be connected to the RF port while the baseband output signal can be extracted from the IF port of the ring mixer.
Saturday, June 10, 2017
180W Pallet Amplifier Using MRF9180
This is my first time to play with the 180W pallet amplifier kit from China. The kit comes with only a printed schematic but there was no details for the input transformer and the coaxial balun. The bias for the LDMOS is not also indicated so I have to download the datasheet of the MRF9180 from the internet.
The input transformer has a 9:1 impedance ratio so it has a 3 turns in the input while a single turn in the output. Connected to the drains are the 25 ohm teflon cables. This coaxial transformer is responsible for stepping up the low impedance drain to approximately 25 ohms. Next is a 50 ohm cable used to combine the 25 ohm balance signal into 50 ohm unbalance at the output. I choose to cut this cable to 15cm so that pallet operation would be optimal at the fm broadcast band.
The datasheet says that for MRF9180, gate voltage bias may be set anywhere between 2 to 4V but in my amplifier the VGS was set to 2.2V. At full output power, the pallet amplifier is consuming around 8 to 10 amps at 24V dc supply.
After the test, I was getting 150W at 144MHz (2W) drive and 200W at 100MHz (1.5W) drive and this pallet amplifier is remarkably broadband. The test was conducted without the LPF at the output.
--- 73 de du1vss.
Sunday, December 18, 2016
7MHz VFO using 3.58MHz Ceramic Resonator
This project is a 7MHz vfo that uses a 3.58MHz ceramic resonator. The oscillator output is fed to a frequency doubler but the output of the stage contains full of harmonics. To clean the output waveform, a double tuned band pass filter is added. Each filter resonates at 7MHz and the passband is quite sharp which effectively attenuate the unwanted harmonics.
The output level is at 3volts peak to peak and has a 60Hz per hour drift after some warm-up. Using 1N4007 as varactor, i was able to tune +/- 0.200MHz from the center frequency of the oscillator. 73 de du1vss
Tuesday, April 5, 2016
QRP RF Voltmeter from your Junk Box
A useful tool that can be easily crafted out from your junk box is this rf voltmeter. I discovered this circuit online and created a prototype out of it. I found this project very useful in reading RMS voltage in my HF /VHF projects. I use it to determine the output power of my rf amplifier, set the null in my balanced modulator, determining the peak voltage output of my oscillator, peaking a band pass filter, etc...
It takes only 3 components to start with. I use 1N60 germanium diode to rectify the high-frequency AC signal into a DC voltage compatible with any digital multimeter. My prototype rf voltmeter is mounted in a small PCB assembled in surface mount fashion. Two connectors soldered on the edge of the pc board to accommodate the positive and negative probe of my digital multimeter.
Connect the alligator clip to the common ground of the circuit you are measuring. Minimize the length of the alligator clip wire to avoid introduction of errors in your measurements, particularly on higher hf bands. In my prototype the lead wire for the alligator clip is just over 6 inches.
When reading the Vrms, take the measurement across the 50 ohm dummy load. For instance, if you measure 13V using your digital tester, the computed power is around 3.38watts, calculated using the formula P = (Vmeasured)² / 50. ---73 de du1vss
Sunday, March 20, 2016
40M DSB Transceiver
The circuit described here is actually a variation of the MDT40 project by VK2DOB, A simple double side band suppressed carrier (DSBSC) transceiver which operates on 7MHz. I find this project simple and a good start if you are interested into home brewing your own rig so I decided to make one.
In the original circuit, it uses a ceramic resonator as a common oscillator for both receive and transmit stage but I have difficulty in finding the parts here in Manila so I decided to use a vfo whose circuit was copied from KD7REM, a rocksteady vfo. Stability is considerable during start up which usually takes less than 30minutes of wam-up and can be used with a couple of QSO without correcting the vfo for a drift. T50-6 toroid was chosen as a core of my inductor where 25 turns of enamel wire was wound. RF feedback was taken at 5 turns from the cold end. I found by experiment that by keeping the capacitance large in the L/C ratio, the oscillator is more stable than the other way around. MPF102 is also used since JFET is more stable than its BJT counterpart.
The balanced modulator and the receiver pre-amplifier stage are constructed together in one board. There are four 1N4148 used in the balance modulator and please note that these diodes are carefully matched by their forward bias voltage. A 500 ohm potentiometer is used to find the null in the balance modulator. Carrier suppression is easily done when you already have completed the transmitter stage since this can be just adjusted by the power output of the rf amplifier stage.
The rf transistors found in the transmitter stage are uncommon so I decided to redesign completely the entire stage using common transistors that are locally available here. 2SC2078 was chosen as the final stage since it is cheap and offers a 4W to 5W ouput at the HF frequencies.
Above is the prototype of my DSBSC transceiver that I made. It is housed in a plastic casing (black) and on the top (grey plastic casing) is the additional 15watts linear amplifier constructed using a push-pull IRF510 mosfet transistor. ---73 de du1vss
Tuesday, December 22, 2015
VHF RF Choke
Home made VHF rf choke. It has a typical value of 0.3uH made by winding 15 turns of 0.2mm enamel wire over a high value resistor (27K 1/2watt) as a former. Inductor leads are soldered across the resistor leads and the instant glue secure the winding on the former.
Most of my home made vhf rf amplifiers uses this rf choke in its bias and also in the DC supply section. Commercial vhf choke generally comes in a small package suitably for smd but since I have so many enamel wires in my junk box, home brew comes in handy. ---73 de du1vss
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